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Bodiam

United Kingdom
41 Posts

Posted - 04 May 2019 :  09:29:17  Show Profile  Reply with Quote
Sorry to be so long posting an update but life has got in the way and I have only just completed the repair. Fitting a new head gasket seems to have fixed the problem, so many thanks to those who suggested this was the fault. The head has been overhauled and hardened exhaust seats fitted - maybe unnecessary but cheap enough to do while the head was off.

My concern over bottoming of the head bolts was not misplaced, the head had been extensively skimmed in the past and the centre bolt on the nearside was too close to bottoming for comfort, so I refitted this with a thicker washer.

Many thanks for the help and advice, on now to the gearbox oil leak and beyond!

It’s good to know that the forum is there to help, I’m sure I will be back.

John
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Bodiam

United Kingdom
41 Posts

Posted - 31 Jan 2019 :  09:41:23  Show Profile  Reply with Quote
Thank you, Jason, that’s really helpful and now very clear what I should be looking for.

Very grateful for the help I’m getting here, I have a feeling you may not have heard the last of me!

John
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JPSH120

United Kingdom
1168 Posts

Posted - 31 Jan 2019 :  09:24:12  Show Profile  Reply with Quote
Face of the head should have notches in it, similar to the one in this image;



If they're not visible, then the head has been skimmed to it's max.
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Bodiam

United Kingdom
41 Posts

Posted - 31 Jan 2019 :  07:56:10  Show Profile  Reply with Quote
Hi, Jim,

Thank you for the reply, I’ll measure up as you suggest and hopefully put my mind at rest.

John
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jimlagos

United Kingdom
205 Posts

Posted - 31 Jan 2019 :  00:11:26  Show Profile  Reply with Quote
I believe that there is indication of amount of skimming by the recesses
machined into the edge of the head itself. I don't know how to load a photo, but hopefully somebody can do some kind of photo or drawing to show what I mean. As for "bottoming" out of the head bolts you can get an idea if you just screw the head bolts into the block until a little bit more than finger tight and measure them? Then check the cylinder head to ensure that they are down enough to clamp the head down.

jim
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Bodiam

United Kingdom
41 Posts

Posted - 29 Jan 2019 :  16:56:13  Show Profile  Reply with Quote
Head off at present for crack testing. A bit concerned that there is no obvious sign of gasket failure, just a general overall deterioration.

The head has had some welding done previously to broaden the land between the water jacket and the edge of the cylinders which is quite narrow and the head has been skimmed after that.

Does anyone know the original depth of the alloy head on a Series 111A? The reason I ask is I have noticed another thread where the owner found the head bolts were bottoming because the head had been skimmed and I’d like to be able to avoid this problem.

Thanks in anticipation for any help.

John
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Bodiam

United Kingdom
41 Posts

Posted - 29 Dec 2018 :  21:48:53  Show Profile  Reply with Quote
Thank you, Glen.

John D
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bigt80

United Kingdom
1051 Posts

Posted - 29 Dec 2018 :  19:50:02  Show Profile  Reply with Quote
Yep; 4lb for the early cars - always seemed v..low :-).
I'd agree head-gasket & just to also confirm that Speedies supply top quality cu/st H.G's for c. £11.50 + the postage. I've used several over the years with no issues. A lot of NOS stuff is not really usable these days. Best of luck with the fix. Cheers. G.
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Bodiam

United Kingdom
41 Posts

Posted - 18 Dec 2018 :  20:58:24  Show Profile  Reply with Quote
Hi, tgr747,

I believe the 4lb cap was fitted to Series I - IIIA cars, increased to 9lb for Series IV to V (unless anyone has better info than I’ve found in the catalogues).

Your post has made me think, though, that I ought to check that the engine in my car is actually the 1600 it started out with before I do anything else.

Thanks for the pointer.

John D
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tgr747

United Kingdom
26 Posts

Posted - 18 Dec 2018 :  19:25:55  Show Profile  Reply with Quote
I am no expert but is 4lbs the normal rad cap for this engine?
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Bodiam

United Kingdom
41 Posts

Posted - 17 Dec 2018 :  20:10:34  Show Profile  Reply with Quote
Thanks for the suggestions Jim, I’ll give them both a try. Won’t be making any more progress before Christmas now, but will post any useful information as I go along.

I’ll certainly have the head crack tested and hope there’s nothing else hiding away!

Best wishes,

John D
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jimlagos

United Kingdom
205 Posts

Posted - 17 Dec 2018 :  19:58:06  Show Profile  Reply with Quote
I've used speedy spares for parts, and also Alpine West Midlands.
Never had complaints about either. If anybody has comments it might be useful.
Good luck.
P.S check carefully for any cracks in the head!


https://www.speedyspares.co.uk/
http://www.sunbeam-alpine.co.uk/

jim
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Bodiam

United Kingdom
41 Posts

Posted - 17 Dec 2018 :  12:18:36  Show Profile  Reply with Quote
Now I’m going to be taking the head off (unless anyone has any 2p washer fixes in mind!) I’d be obliged if you could recommend a supplier of a good quality head gasket set.

I come from the world of Triumph TR’s, where there is so much Chinese junk on the market (and I don’t mean their boats) that inside information on quality is invaluable.

Thanks in anticipation,

John D
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Bodiam

United Kingdom
41 Posts

Posted - 17 Dec 2018 :  10:10:05  Show Profile  Reply with Quote
Good morning, Jim, thank you for the reinforcement.

I guess it was hoping for too much that someone would have had a similar experience and fixed it with a 2p washer!

Head off is no bad thing anyway, the car hasn’t been converted to unleaded so that would be a good excuse to get it done.

Thanks again, John

John D
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jimlagos

United Kingdom
205 Posts

Posted - 17 Dec 2018 :  08:40:25  Show Profile  Reply with Quote
Good morning.
99.9% sure it's head gasket!

jim
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